The
Rush Derailment
5
January 1963
Aidan
Langley CEng MIET MIEI
To
those who have read ‘Red for Danger’ by LTC Rolt, you will be familiar
with how often a combination of seemingly inconsequential events and
circumstances have ended in a catastrophic railway accident with multiple
fatalities. Therefore, I was surprised to find that, in 1963, there had been
a railway incident at Rush & Lusk station, where I start my commute
every morning. Perhaps the most surprising of all is that almost everybody
involved walked away from the accident, and very few of the people I stand
on the platform with each morning are aware that the incident happened at
all. The opening sequence of events are truly reminiscent of many of the
unfortunately ending scenarios in Rolt’s body of work.
CONTEXT
Rush
& Lusk station today is a busy commuter station on the Northern main
line, serving a population of around 17,000, with some 26 services a day,
not counting through trains, both to and from Dublin city. Both Up and Down
platforms are situated south of Overbridge OB39 carrying the R128 Rush to
Lusk road. The station is on an uninterrupted section of track with no
crossovers or sidings between Donabate to the south and Skerries to the
north.
By
contrast, in 1963 the population was largely agrarian, as a traditional
centre of market gardening, with only some 3,000 inhabitants. Rush had its
own signal box controlling crossovers to the north and south of the station,
and where the car park is now located, there was a siding off the Up line,
from which the fresh produce of both Rush and Lusk was sent to the Dublin
markets. The Up and Down Platforms were shorter, but both extended north of
OB39, as shown in Figure 1, although the station buildings were all in the
same location as they are today. The footbridge, however, was added after
the incident.
SEQUENCE OF EVENTS
The
14:15 ex-Belfast train, comprising B160 (locomotive), 3133 steam-heating
van, and former GNR(I) coaches N406, N328, N372, N404, N196, N612, had
departed Dundalk at 16:15 on Saturday, 5 January 1963. It was 15 running
minutes late. As was practice at the time, a CIÉ-owned diesel electric
locomotive and a steam-heating van had been coupled to the consist at
Dundalk to replace the UTA steam locomotive which had hauled the train from
Belfast. After the train had been made up in Dundalk it was checked by Train
Examiner Thomas Mullen. This included tapping all the wheels on the
left-hand side of the train, but he did not notice anything wrong with the
tyres; the brakes were hard on at this time. He did notice a dynamo belt
missing off Coach N404 which he made note of. When the train departed
Dundalk, there were in fact 4 people on the footplate, two trainee drivers,
an Amiens St. Locomotive Inspector, and the regular driver.
As
is the case with the Enterprise
today, the only stop between Dundalk and Dublin was at Drogheda, and the
train made up a minute on the timetable with nothing remarkable happening.
The train departed Drogheda at 16:44 and proceeded south nonstop through
Laytown, Mosney, Gormanstown and Balbriggan travelling at between 50 and
60mph. Passing through Skerries, the train was travelling at around 60 mph
dropping to 50 mph cresting the bank between Skerries and Rush, and as it
approached Rush, at about 17:00, was travelling at around 65 mph. From the
account of those on the footplate, when, as the locomotive drew level with
the Rush & Lusk Stationmaster’s Office, there was a ‘bang’ and the
engine ‘lurched’, then the brakes were applied automatically and the
locomotive was brought to a halt, after about 700 yards, just beyond OB38
(Rogerstown Lane) south of the station. (See Figure 3).
From
the perspective of the station, there were mercifully no other trains due at
the time, and no one exposed on the platforms. The signalman, having
previously booked on at 16:30, had heard the train approach. The line is in
a relatively deep but straight cutting as it approaches the station, and he
had heard a ‘rumbling and thudding’ noise, and when he looked down the
track saw the train ‘beginning to tilt’, he saw a ‘blue flash’ and
the train divide, with sparks coming from the rear of the front portion of
the train. The rear portion of the train decelerated more rapidly than the
front portion, being derailed and ploughing to a stop after 240 yards, still
within the station area.
From
the accounts of the witness statements, all the key actors performed their
assigned roles correctly. At 17:03, the signalman sent the Obstruction
Danger signal to the Malahide and Skerries signalmen, (Donabate being
switched out at the time), followed immediately by the Train Divided signal.
The
Guard, having being in the rear portion of the divided train, was thrown to
the floor of the carriage as it came to rest. He first checked the occupants
of the carriage he was in, then alighted onto the Up platform, and, having
checked that the rest of the passengers in this portion of the train were
uninjured, went to the signal box to check that the scene was protected. A
party set out in both directions to lay detonators on the Up and Down lines,
whilst calls were made to the Gardaí, rescue workers and platelayers.
Having confirmed the site was protected by signals, the guard detrained the
passengers in the rear portion onto the Down line as the carriages were
tilting so far that alighting onto the Up platform was not practical. From
reports there was no panic, a number of passengers offering assistance to
others also assembled on the Down platform
The
situation with the front portion of the train was similar; the train was
largely on the rails, with the exception of the trailing bogie of the
rearmost carriage N328. The crew kept the passengers onboard the train
initially, moving them from the completely dark carriage N328 to the
undamaged N406. This portion was some ¼ mile beyond the station and not
within sight of the station or signal box. The Guard arrived at the scene
and arranged for the passengers from the front portion to be led back along
the line to the station and a cart be sent to carry passenger luggage back
to the station.
Given
the season and the time of day, it was dark and below freezing; January and
February 1963 was one of the coldest two-month periods since records began,
with a ‘blocking high’ over Scandinavia. There had been heavy snow
during the last week of 1962, although there was no snow on the ground at
the time of the incident in Rush. The following week, temperatures dropped
to -10°C, although weather was not mentioned in the enquiry report. The
mean temperature in the area for the 24 hours of 5 January was 2.5°C
(36°F).
CONSEQUENCE
OF INCIDENT
As
previously mentioned, the front portion of the divided train was largely on
the rails. The 2nd carriage (N328) had been torn from its trailing bogie, so
that the coach frame was sitting on the rails (see Figure 3), having been
dragged for almost a ½ mile, and thus having caused some minor damage to
the cross-over at the south end of the station and other infrastructure on
the permanent way.
The
rear portion of the divided train had a much more spectacular arrest. The
trailing bogie from coach 328 had become entangled in the leading bogie of
coach N372 (see Figure 4), derailing it. This resulted in coach N328
striking the Up platform, tearing away the coping stones, and ploughing up
the permanent way before coming to rest. The rear two vehicles then struck
the displaced coping stones and were also derailed. (See Figure 6).
INVESTIGATION
AND ROOT CAUSE
The
CIÉ Inquiry found that the derailment was caused by the ‘fracture of the
tyre on the left-hand wheel of the leading axle of the trailing bogie on
coachN328.’ (See Figure 5 & 6). The wheel was of the tyred type in use
at the time. As a result of the tyre break, there was no flange, the
wheelset had derailed, to the left in the direction of travel. Witness marks
found north of the station were presumed to be the point at which the
incident started, and a photograph shows the witness mark of the right hand
flange striking the sleepers approaching Rush (see Figure 7). The train may
have proceeded unimpeded in this manner, except that the right hand wheel
was not captured by the check rail of the cross-over at the north end of the
platform, and instead was guided by the trailing point blade towards the
platform. The force of the collision with the platform is presumed to have
torn the bogie, now fully derailed, from the coach, with the subsequent
coaches following as the permanent way was broken up in their path. No
reason was offered for the cause of the tyre fracture. The components were
sent to the British Transport Research Department in Derby. The result of
the metallurgical testing, released the following May, found that there was
no pre-existing corrosion, obvious crack initiation point, or other latent
defect in the tyre.
Subsequent
investigation found the cause to have been a loose ‘Gibson Ring’. The
Gibson ring was developed by J Gibson of the GWR, Wolverhampton, who retired
in 1864. As Figure 8 below shows, the Gibson ring is a profiled ring. To
assemble it the tyre is first heated, then attached to the wheel, and the
Gibson ring is inserted. Whilst hot, the inner profile of the tyre is then
‘crimped’ to deform around the ring and secure it. It could be
determined at that stage, but the suggestion was that either during the
wheel assembly operation or during manufacture, there had been some defect
in the ring, which caused it to fail over time. The tyre would then have
been no longer fixed, and would have been able to rotate independently of
the wheel and move laterally. The fact that the brakes were on when the
wheels were ‘rung’ in Dundalk could have obscured the fact that there
was a defect, or possibly the failure occurred after leaving Dundalk.
From
the description of the incident and the photographs available, it is clear
that the incident could have had much more disastrous consequences. Apart
from the absence of people in the path of the wreckage, or any other traffic
on the line, if the derailment had happened even a mile further south, it
could have resulted in a portion of the train ending up submerged in the
Rogerstown Estuary between Rush and Donabate or the Broadmeadow Estuary
between Donabate and Malahide.
If
the Up platform had not been present to guide the derailed coaches, they
could have deviated further out of gauge and struck the pillar of the
Overbridge OB39, resulting in a much more sudden deceleration of the
coaches, and possible harm to passengers.
REACTION
TO THE INCIDENT:
The
fact that the incident happened on a Saturday evening may have reduced
interest, as it didn’t affect weekday traffic. Traffic was restarted with
single line working the following evening at 19:00, only 25 hours after the
incident, and a normal timetable, albeit with single line working on the
Down line only, from 02:15 on the Monday morning. The Up line was opened
again the following Sunday, 13 January. As a result, the impact of the
incident on the wider community was limited. Reporting of the incident
nationally was a single article in the Irish
Times, noting that there were delays, and a British Pathé news crew
filmed the recovery operation. For the people of Rush, the incident was
noteworthy. Speaking to residents of Rush who were around at the time, they
vaguely remember it having happened, but the impact was very limited.
CONCLUSION
All
the elements were in place in Rush for a truly horrific incident. In many
ways the incident was similar to the Eschede Deutsch Bahn ICE incident of
1998:
•
The cause was identified as a catastrophic wheel failure,
•
The train was travelling at speed, (albeit slower) with carriages
outside of gauge,
•
There was a crossover which aggravated the derailment,
•
The derailment happened just before an overbridge.
In
the case of Rush, as mentioned, the key actors performed their duties
effectively and per the Rule Book. Signals were sent, protection put in
place, and order maintained in what in today’s parlance is the
‘Preservation of Life’ phase of the incident.
As
stated earlier in this piece, there was no conclusive root cause identified;
however it can be speculated that there was some issue with the Gibson Ring,
either a defect on assembly or a manufacturing flaw which caused it to fail.
Current practical use of Gibson Rings by heritage railways has demonstrated
they can operate effectively even when fitted incorrectly, certainly at the
low speed at which most heritage railways run.
The
decision to phase out two-part wheels on rolling stock had already been
taken when the Rush & Lusk derailment happened, but it can be said that
the process of moving towards monobloc wheels was hastened by the incident.
Reviewing
the incident and how it unfolded, highlights just how important seemly
trivial details are, how the correct following of processes are vital, and
how learning the correct lessons from past incidents can help prevent
serious incidents from being catastrophic.
SOURCES
CIÉ
Report of Enquiry into the cause of Derailment at Rush, 5 January 1963
National
Library of Ireland Photo Archive, O’Dea Photograph Collection
Met
Éireann Exceptional Weather Events Jan-Feb 1963
Discussion
with J.C. Pemberton, Irish Rail (Retired)
Discussion
with Gerald Beesley
Casey
and Ryan families of Rush, Co Dublin
South
Devon Railway Engineering Ltd.
Additional
research by Tom Normanly.